1. Inner check valve: the check valve inside the valve body is to insure the hydraulic oil will not be returned. 2. Inner relief valve: the relief valve inside the valve body is able to adjust the hydraulic system working pressure. 3. Oil way: parallel circuit, with power beyond. 4. Control way: manual, air, air&electric, micro-switch, electric&hydraulic control. 5.Valve construction: monoblock construction, 1-8 levers are available to assembled as you requests. 6.Spool function: o, a, y , p etc. 7. Flow 40 l/min with pressure 160bar, 200bar, 315bar 8.Spool returning type with t (spring return) and w (ball locking) 9. Joining port: l (screw connection) 10 .Nominal diameter: g1/2; g3/8; m18*1.5
Gerrard, a Spanish hydraulic customer who just repeated the order at the end of May, repeated another order for hydraulic pressure valve again today, with total 3 orders for a hydraulic pressure valve a year. Since Gerrard chose AAK hydraulic valve, his customers are very satisfied with the accuracy and stability of AAK hydraulic valve. The market sales volume has increased by nearly 30% year-on-year. Now he has a higher and higher position in the company. I still remember that Gerrard urgently needed to purchase a batch of hydraulic pressure valves for cranes. However, due to the high requirements for inner hole accuracy, he visited more than 10 hydraulic valve manufacturers, and none of them could reach around 1�¼m error requirement. Gerrard was very anxious. Fortunately, some peers brought Gerrard into contact with AAK. Finally, AAK helped to solve the problem of inner hole accuracy of hydraulic pressure valve smoothly. 3 months before Gerrard got into touch us, AAK HYDRAULIC VALVE purchased a honing machine imported from the United States to deal with the production of special orders. After repeated exploration for more than a month, modified the fixture of the equipment ourselves, we created the most consistent SOP to ensure the 1 �¼M accuracy error of the inner hole for the hydraulic pressure valve. At present, less than 5% of the domestic hydraulic valve manufacturers are equipped with this equipment. Among these 5% of hydraulic valve manufacturers, maybe only one manufacturer, we AAK HYDRAULIC VALVE, can modify the equipment on our own. When AAK HYDRAULIC VALVE promised Gerrard that we have 90% of confidence to ensure that the inner hole accuracy of the hydraulic pressure valve can be controlled at 1 �¼ M, he was uneasy. After all, he visited more than 10 hydraulic valve manufacturers, and none of them successfully controlled the inner hole accuracy of the hydraulic pressure valve to 1 �¼mã??Gerrard also was in doubt. We can understand him, because we haven't done the hydraulic pressure valve with inner hole accuracy error controlled at 1 �¼ M before. After 15 days of sending the sample, Gerrard emailed us that the sample of AAK hydraulic pressure valve was approved at one time, and the surface finish of the hydraulic pressure valve was also praised by his clients. Subsequently, the first hydraulic pressure valve order from him was successfully completed. AAK hydraulic pressure valve has two absolute advantages in controlling inner hole accuracy: 1. AAK HYDRAULIC VALVE has advanced equipment - honing machine, which is refitted by ourselves to ensure that the inner hole accuracy of the hydraulic pressure valve can be controlled at 1�¼m. 2. AAK HYDRAULIC VALVE has targeted operation process, can realize the personalized customization demand for the inner hole accuracy of hydraulic pressure valve, which can not be achieved by 95% of domestic hydraulic valve manufacturers.
Kate, the buyer of Terex company, was asked by the head office last month to purchase a batch of hydraulic pressure valves within 3 months. She vowed to the owner that it would be completed in 2 months. As usual, Kate sent the hydraulic pressure valve inquiry to more than 10 hydraulic valve manufacturers she was familiar with, including American hydraulic valve manufacturers and Chinese hydraulic valve manufacturers. She chose 3 factories to provide hydraulic pressure valve samples for testing. After the test, the technical department informed that only the hydraulic pressure valve samples provided by American manufacturer were qualified. The trouble is that the price of the qualified hydraulic pressure valve exceeds 40% of the company's budget price. She has no authority to decide to use the products of this American hydraulic valve manufacturer. After discussion with the technical department, she learned that those unqualified hydraulic pressure valves are mainly due to the wear or fracture of the sealing ring after 15,000 times of impact during the durability test of the hydraulic pressure valve, resulting in the leakage of the hydraulic pressure valve. Only those hydraulic pressure valves that have not leaked for more than 40,000 times are qualified. She was very depressed that the quotation of the other 3 hydraulic pressure valves was within the budget, but the quality was unqualified. At this time, Kate realized why the company gave him 3 months to purchase. She hurriedly sent inquiry to new hydraulic valve manufacturers, and specially emphasized the need for hydraulic pressure valves with more than 40,000 durability tests. The trouble is that no hydraulic valve manufacturer gave her an offer. Kate realized the difficulty of procurement. She had wasted 3 weeks. Procurement was still in its infancy, and the technicians had been urging progress. After learning about Kate's purchase status, the colleague recommended her to contact AAK HYDRAULIC VALVE to try. When we received the hydraulic pressure valve drawing from Kate, we first gave a quotation. She told us very frankly that the price of AAK was 20% higher than that of other China hydraulic valve manufacturers, but 15% cheaper than that of the United States. She needed us to reduce the price greatly. We suggested providing the hydraulic pressure valve samples for testing first, and then discuss the price after passing the test. 2 weeks later, Kate informed that the test was qualified and AAK hydraulic pressure valve durability test had reached more than 40,000 times. She was surprised why AAK passed the hydraulic pressure valve durability test, while the other hydraulic valve manufacturers in China failed. AAK hydraulic valve was also eliminated by customers 2 years ago because the durability test of hydraulic pressure valve failed to meet the standard.
Just yesterday, I received a repeat order from Andy for a hydraulic flow control valve, which is just 3 months away from the delivery time of the last batch of hydraulic valves. The American customer Andy, started to communicate with us in 2019. Maybe it was just not the right time, we still didn't partner with each other till the beginning of this year. Because of encountering a Waterloo at the previous hydraulic valve manufacturer, he turned the tables at AAK and regained his confidence. At the end of last year, Andy purchased a batch of hydraulic flow control valves from a hydraulic valve manufacturer. Because 20% of the shipments leaked, he encountered customer claims. The old hydraulic valve manufacturer was unwilling to bear the claim or re-produce. The customer kept pushing for replacement hurriedly. The owner asked him to find a high-quality hydraulic valve manufacturer to reproduce the goods for the customer. Andy had a big headache at that time. The replacement quantity is not big, the hydraulic valve manufacturers with exquisite quality were unwilling to produce the small quantity for him. The hydraulic valve manufacturers who were willing to produce this quantity, were not able to meet the customerâ??s requirement about the roughness of hydraulic flow control valve. He ran into a wall everywhere, which made Andy haggard. When Andy contacted with AAK HYDRAULIC VALVE, we are willing to cooperate with her to solve this difficult problem. We tested the leaked hydraulic flow control valve sample. The reason for the leakage is the roughness of the mounting surface of the hydraulic flow control valve. According to the customer's service conditions, this roughness must be controlled at 1.0 �¼ M or less. Andy is very confused why 80% of the installation surface roughness of hydraulic flow control valve is up to standard, while 20% is out of this range. The root of this fluctuation is the master's operation method, resulting in human error. The surface roughness is the depth, density, texture of the traces left on the machined surface from the action between the tool and the part surface, which depends on the master's processing technique. Andy is very clear that at present, most domestic hydraulic valve manufacturers generally control the roughness of the installation surface of hydraulic flow control valve at 0.8-1.0 �¼ m. The biggest problem is not stable enough. Andy also knows that only AAK controls the roughness value of hydraulic flow control valve within 0.8 �¼ M, which can completely avoid leakage outside the hydraulic flow control valve, because of rest assured, Andy decided to repeat the order with AAK HYDRAULIC VALVE.
Just yesterday, I received a repeat order from Andy for a hydraulic flow control valve, which is just 3 months away from the delivery time of the last batch of hydraulic valves. The American customer Andy, started to communicate with us in 2019. Maybe it was just not the right time, we still didn't partner with each other till the beginning of this year. Because of encountering a Waterloo at the previous hydraulic valve manufacturer, he turned the tables at AAK and regained his confidence. At the end of last year, Andy purchased a batch of hydraulic flow control valves from a hydraulic valve manufacturer. Because 20% of the shipments leaked, he encountered customer claims. The old hydraulic valve manufacturer was unwilling to bear the claim or re-produce. The customer kept pushing for replacement hurriedly. The owner asked him to find a high-quality hydraulic valve manufacturer to reproduce the goods for the customer. Andy had a big headache at that time. The replacement quantity is not big, the hydraulic valve manufacturers with exquisite quality were unwilling to produce the small quantity for him. The hydraulic valve manufacturers who were willing to produce this quantity, were not able to meet the customer's requirement about the roughness of the hydraulic flow control valve. He ran into a wall everywhere, which made Andy haggard. When Andy contacted with AAK HYDRAULIC VALVE, we are willing to cooperate with her to solve this difficult problem. We tested the leaked hydraulic flow control valve sample. The reason for the leakage is the roughness of the mounting surface of the hydraulic flow control valve. According to the customer's service conditions, this roughness must be controlled at 1.0 M or less. Andy is very confused why 80% of the installation surface roughness of hydraulic flow control valve is up to standard, while 20% is out of this range. The root of this fluctuation is the master's operation method, resulting in human error. The surface roughness is the depth, density, texture of the traces left on the machined surface from the action between the tool and the part surface, which depends on the master's processing technique. Andy is very clear that at present, most domestic hydraulic valve manufacturers generally control the roughness of the installation surface of hydraulic flow control valve at 0.8-1.0 m. The biggest problem is not stable enough. Andy also knows that only AAK controls the roughness value of hydraulic flow control valve within 0.8 M, which can completely avoid leakage outside the hydraulic flow control valve, because of rest assured, Andy decided to repeat the order with AAK HYDRAULIC VALVE.
It took 3 months and 6 proofing adjustments to match the sample quality of hydraulic pressure control valve made in Germany. Finally, AAK passed the parameter test of hydraulic pressure control valve, and our hydraulic pressure control valve was affirmed by Eatonâ??s company. We became Eatonâ??s first supplier for hydraulic pressure control valve in China. In mid October last year, an agent of Eaton came to AAK HYDRAULIC VALVE and brought a sample of Eaton hydraulic pump with a purchase value of more than US$150,000.00, asking us to make a quotation. After we checked the product parameter requirements of the artwork, we declined the quotation because AAK is only good at hydraulic valve products. Compared with its domestic peers, most of the technologies of AAK HYDRAULIC VALVE were in TOP 1-6. We thought Eaton agent would not consider us again. However, after a month, he came again and brought a Vickers Series solenoid valve with a value of up to US$200,000.00. We directly said that we are not good at this kind of products and couldn't quote. Eaton agent saw that we rejected the products that AAK is not good for 2 times, he felt that AAK is different from other hydraulic valve manufacturers, and recognized the professionalism of AAK HYDRAULIC VALVE. For the 3rd time, he brought a sample of pilot hydraulic pressure control valve with very high precision and wanted to test the parameters with our pressure test bench. I realized that Eaton agent actually wanted to test our pressure test bench with his samples. It was the first time for us to encounter such a situation, the purchaser did not test the quality of AAK hydraulic valve, but tested the equipment producing hydraulic valves first. Being satisfied with our pressure test bench, he asked if we were interested in this pilot hydraulic pressure control valve, which was a hydraulic pressure control valve produced in Germany. After learning the parameters of the hydraulic pressure control valve in detail, AAK HYDRAULIC VALVE technical team discussed the artwork of the hydraulic pressure control valve. We were 90% sure to match the quality of this hydraulic pressure control valve produced in Germany. More than 20 days later, we sent the first approval sample of the hydraulic pressure control valve. The sample comments was that there was still a 12% difference between the accuracy of AAK hydraulic pressure control valve and that of German hydraulic pressure control valve. We were required to send the revised sample again. The whole proofing and approving process have been bumpy, the parameters were continuously required to be improved. The samples have been adjusted for 6 times, finally, it met the quality of the German hydraulic pressure control valve after 3 months.
The hydraulic pressure control valve is high pressure resistant with over 2 million times of service life, AAK won the order back at a high price Caspar is from Samhydraulik S.p.A. in Italy, mainly responsible for the purchasing of hydraulic valves. In March this year, Caspar requested AAK to sample 10 hydraulic pressure control valves by soonest. This sample order was quoted half a year ago. There must be a reason for him to be so anxious to place an order now. After several rounds of communication, it was learned that Caspar was cheated by the original hydraulic pressure control valve manufacturer. In the second half of last year, their company developed a new hydraulic power unit, which requires a high-pressure hydraulic pressure control valve, and the durability should reach more than 2 million times. Caspar contacted more than 10 hydraulic pressure control valve manufacturers. Most of them are able to produce the hydraulic pressure control valves with high pressure resistance and durability of more than 2 million times. Only AAK hydraulic valve and other 2 manufacturers have quoted prices. After receiving our quotation, Caspar said that the price of AAK hydraulic pressure control valve was about 20% higher than that of other manufacturers, and then there was no further news. Until today, 6 months later, he was anxious to ask AAK to make samples immediately. 6 months ago, Caspar selected another hydraulic pressure control valve manufacturer to make samples. 5 weeks later, their new hydraulic power unit was successfully tested and the equipment was expected to be popular. Caspar asked the original hydraulic pressure control valve manufacturer to hurry up to prepare materials, but the manufacturer wanted to raise the price by 40%. Because the valve spool material was hard, the cutting tools needed to be changed constantly, the production cost was increased, and the defective rate was also high. If without a price increase, the manufacturer refuses to produce the order. Caspar felt very helpless. The boss was very dissatisfied with such a hydraulic pressure control valve manufacturer who raised the price at the last moment, and asked Caspar to find a new manufacturer. Caspar suggested that AAK can make samples. If the original price of AAK hydraulic pressure control valve can be maintained, 20% of the cost will be saved. 1 month later, AAK sent 10 samples of hydraulic valve pressure control valves. 1 week later, Caspar informed that the test was passed and 1,000 samples need to be produced immediately. Caspar also wants to know why AAK hydraulic valve pressure control valve can maintain its original price in the same 6 months, while the other manufacturer needs to increase it by 40%. Most manufacturers of hydraulic pressure control valves do not pay attention to some details in the processing at the drawing stage, and only know after suffering in the sampling process.
Lucas is from a Canadian hydraulic equipment company. He found AAK hydraulic valves online last September. His first inquiry was the hydraulic pilot-operated pressure control valve. After 3 rounds of email communication, he placed a trial order for 20 pcs of hydraulic pilot-operated pressure control valves. I received the order so smoothly, but I didn't expect that AAK would almost take the blame for others in the first cooperation. At the beginning of last month, Lucas informed by email that there were problems with all 20 hydraulic pilot-operated pressure control valves provided by AAK. When the equipment was installed and debugged, the hydraulic system went on strike. This is the first time I have encountered such a complaint. AAK will do various tests on each hydraulic pilot-operated pressure control valve before leaving the factory, and deliver it only after it is qualified. I asked the engineer and the workshop to verify. It was proved that the programming and production of the hydraulic pilot-operated pressure control valves are completely consistent with the drawings provided by Lucas, so I can ensure that the samples of AAK hydraulic pilot-operated pressure control valves are qualified. Our engineers speculate that there may be a problem with the oil circuit design of the valve block system, but Lucas engineers believe that AAK is shirking the responsibility. So I suggest Lucas try the hydraulic pilot-operated pressure control valves of other manufacturers to debug. If the hydraulic system is still abnormal, our guess is right. Two weeks later, Lucas frankly told us that there should be a problem with the oil circuit design and asked us what good methods we had? The next day, Lucas sent us the video of equipment commissioning. Indeed, during the operation of the equipment, the speed increases when the cylinder of the hydraulic system is lowered, which is equivalent to the increase of flow, and the original set pressure of the hydraulic pilot-operated pressure control valve will also increase, resulting in the instability of system pressure. Therefore, it is inferred that the instability of pressure is caused by the thin oil passage of the hydraulic valve block in the system. We suggest that he send us the schematic diagram of the hydraulic system. After analysis, AAK engineers believe that the oil circuit design cannot match the working conditions of the equipment. AAK plans to design and process a new hydraulic valve block, and then installs the AAK hydraulic pilot-operated pressure control valves to debug the equipment. If it is not successful, AAK will not charge any fee for the hydraulic valve block. A month later, AAK sent out the newly designed hydraulic valve block. Lucas sent an email 3 days after receiving AAK hydraulic valve block. He informed that after installing the AAK designed hydraulic valve block and the hydraulic pilot-operated pressure control valves, the hydra
HIGINSON company plans to develop a new plunger hydraulic cylinder, which needs to purchase the supporting hydraulic directional control valves. Helen, who had just joined the company, stumbled when purchasing the hydraulic directional control valves. Helen has no hydraulic valve supplier and can only purchase from the original hydraulic valve manufacturer of the company. Half a month later, the engineer and technician of the company installed the hydraulic directional control valves purchased by Helen for commissioning, and the plunger hydraulic cylinder dropped intermittently with vibration and noise. The technician pointed out that the hydraulic directional control valves needed to be replaced. Helen contacted the original manufacturer of hydraulic directional control valve. Per the manufacturer, the delivered hydraulic directional control valves met the requirements of Helen's parameters, and the accuracy also fully met the standard. As a novice, Helen was helpless, and the technician did not specifically say why to replace the hydraulic direction control valves. She tried to contact the new hydraulic directional control valve manufacturer to solve the problem. Helen left a message on AAK website: why is the plunger hydraulic cylinder equipped with hydraulic directional control valve noisy? At this moment, we can't tell the reason. After communicating with Helen, I learned the process of purchasing this hydraulic directional control valve and the judgment of technician in their company. AAK engineers are not 100% sure that where the problem is according to the hydraulic directional control valve drawings sent by Helen, the shipment sample of the original manufacturer and the video of their technician's machine test. We are thinking if Helen, as a novice, has mistaken the type of hydraulic directional control valve? The hydraulic directional control valves can be divided into internal leakage type and external leakage type. Combined with the working conditions, this plunger hydraulic cylinder just reverses the oil outlet chamber, and the back pressure is high. If the internal leakage hydraulic directional control valve is used, there will be abnormal phenomena such as vibration or noise. We told Helen our thinking. She really did not note to the original manufacturer that the hydraulic directional control valve is internal leakage or external leakage. I told her that AAK has ready-made samples of the external leakage hydraulic directional control valve. It is recommended to test the machine with AAK hydraulic directional control valve to see if there is still vibration or abnormal noise. A week later, Helen sent an email saying that AAK hydraulic directional control valve was installed and there was no abnormality in the test run.
AAK Hydraulic Flow Control Valve with 3 major advantages, recognized by Yagmur Yagmur is from T�¼rkiye and mainly purchases hydraulic cartridge valve standard parts from Ningbo. Recently, they developed a hydraulic drilling equipment that uses hydraulic flow control valves that are modeled after HydraForce standard parts, and purchased from a hydraulic valve manufacturer in Ningbo. During equipment debugging, it was found that the flow rate of the hydraulic flow control valve was unstable, and the leakage rate did not match the hydraulic system. The original hydraulic flow control valve manufacturer stated that this is a replica of HydraForce and is unwilling to optimize its function for several hydraulic flow control valve samples. Yagmur checked with several other hydraulic valve manufacturers, but they were not interested. Yamour was very anxious. The original hydraulic flow control valve manufacturer introduced AAK to Yagmur. After communication, it was learned that her requirements for this model include low leakage and high precision requirements for valve holes. Based on the hydraulic system schematic provided by her and the industry model code of the HydraForce hydraulic flow control valve, I recommended a ready-made sample to her. As long as the external dimensions meet his manifold requirements, it can solve the problem she is currently facing. 2 weeks after the sample was sent out, Yagmur informed via email that the drilling equipment was successfully debugged. The low leakage of AAK hydraulic flow control valve meets their system requirements, especially the flow control function that they are very satisfied with. I told her that for this AAK hydraulic flow control valve, we have 3 major advantages: 1. The internal leakage of AAK hydraulic flow control valve is 5 drops/min, while most peers can only achieve 8-10 drops/min. 2. The hole accuracy of AAK hydraulic flow control valve can reach IT6-IT7 level, and the surface roughness can reach Ra0.2-0.025m. 3. The AAK hydraulic flow control valve function fully aligns with the standard parts of HydraForce, and there are probably no more than 3 manufacturers in Ningbo to meet it. The vast majority of hydraulic flow control valve manufacturers in the industry do not use forming cutters for machining small quantities of hydraulic flow control valves, but use CNC instead to process according to dimensional requirements. The result of this machining is an accuracy of 0.03mm and a positional tolerance of 0.02mm. The AAK hydraulic flow control valve is processed with forming tools, and the dimensional accuracy of the valve hole after processing reaches 0.01mm, with a positional tolerance within 0.007mm. At the same time, AAK has its own standards for tool selection, with hardness of HRA90 alloy material, heat resistance of 900 , valve hole accuracy of IT6-IT7 level, surface roughness of Ra0.2-0.02m, and tool life is 30 times higher than ordinary alloy steel.
The original manufacturer cannot handle RV12-26 hydraulic pressure control valve with special requirements, and AAK solved it with 2 strict processes A few days ago, Anthony from Spain needed to purchase a hydraulic screw-in cartridge pressure control valve equivalent to HydraForce RV12-26, but with a special requirement for the accuracy of the valve cage. Anthony chose a hydraulic cartridge valve manufacturer in Ningbo China who had cooperated with him for 2 years. However, the accuracy of the valve cage for RV12-26 hydraulic pressure control valve was unstable. The original manufacturer made samples for 3 times and all failed. 2 months have been wasted, and the engineer was very dissatisfied. Anthony was very frustrated. Last week, Anthony browsed the website of AAK hydraulic cartridge valve manufacturer on B2B and left a message: 1. Do you have procedure for RV12-26 hydraulic screw-in cartridge pressure control valve? 2. Can the valve cage of hydraulic pressure control valve be customized with special requirements? 3. Can you ensure that the valve cage of each hydraulic pressure control valve meets the accuracy requirements? After communication, we learned that Anthony encountered a problem with the accuracy of the hydraulic pressure control valve cage when purchasing from the original hydraulic cartridge valve manufacturer. In response to his special requirements, we provided 2 suggestions: optimizing the precision machining of the valve cage and conducting 100% independent testing of the valve cage accuracy. Anthony asked, how does AAK detect the accuracy of valve cages? First, I told Anthony that accuracy is not determined by testing, but rather by precision machining. For valve cage with special requirements, focus on precision machining only cannot avoid potential problem completely. At this point, testing is to eliminate the hidden problem, and the original hydraulic cartridge valve manufacturer may have overlooked this detail. The valve cage of this hydraulic pressure control valve can be precision machined using the TOYODA cylindrical grinder from Japan. The stable grinding accuracy is the best among our experienced technicians, not only high in accuracy, but also stable. Especially low vibration bed and high-precision feed mechanism, combined with specialized cutting fluid, the processed hydraulic pressure control valve cage has a clear contour and a surface finish of within Ra0.2�¼m, the dimensional accuracy tolerance is within 0.5�¼m. Regarding the inspection of the hydraulic pressure control valve cage, please refer to the video of our workshop's on-site operation. This is a KEYENCE measuring instrument imported from Japan, which is equipped with a 20 megapixel CMOS laser probe. Before testing, our QC first inputs the size requirements of the valve cage into the program, then places the valve cage into the platform.
The service life of hydraulic flow control valve is more than twice that of the original manufacturer, Shirley has sent more and more inquiries to AAK Shirley comes from a hydraulic equipment company in the United States, who is an old employee of the company. She rarely fails in purchasing, and her cooperation with AAK is tepid. It was not until the cartridge hydraulic flow control valves purchased last year failed that she learned that AAK Hydraulic Valve was different from other hydraulic cartridge valve manufacturers, and now she is sending us more and more inquiries. At the beginning of the year before last, Shirleyâ??s company sold the hydraulic power unit for metal extrusion equipment. Less than half a year, customers complained that the pressure of the power unit was abnormal, and even went on strike. During after sales service, it was found that the leakage was caused by the serious wear of the hydraulic flow control valve sleeve, resulting in abnormal equipment pressure. The original hydraulic flow control valve manufacturer replied that under the high-pressure working condition of 450bar and high-frequency use, it is unavoidable for the hydraulic flow control valve sleeve to be worn and the only solution is to replace with new one for free, but 5 months later, the same problem occurred again. The customer was not satisfied and complained directly to the boss. The boss was surprised that an old hand like Shirley would stumble. After investigation, it was found that this hydraulic valve manufacturer who had cooperated for 5 years ignored the details of high pressure and high frequency. The boss asked her to change the manufacturer and replace those severely worn hydraulic flow control valves as soon as possible. Shirley thought of AAK, because at the beginning of the inquiry, AAK mentioned that this hydraulic flow control valve had special working conditions, if the material selection was not proper, it would be impossible to use it for 1 year or more. After learning of Shirley's procurement dilemma, AAK urgently produced 50 hydraulic flow control valves within 1 month for them to replace the current ones. 6 months after the trial order was delivered, Shirley informed us by email that the equipment installed with AAK hydraulic flow control valve was working well without any abnormalities, and I said there would be no abnormalities even in 1 year. Shirley admired the confidence of AAK Hydraulic Valve in quality, and ordered another 300 hydraulic flow control valves. Under the high-pressure condition of 450bar, to get the hydraulic flow control valve used in high frequency a service life of more than 1 year or 2million times, AAK Hydraulic Valve uses 3 advantages to exceed peers. 1. The valve sleeve of AAK hydraulic flow control valve adopts 18Cr2Ni4WA high-strength alloy carburized steel. During heat treatment, carburize at 900~920 , temper at 600~650
3drops/min hydraulic flow control valve, AAK got back the reorder at a high price Margaret, from India, is an old hand in the procurement of hydraulic components, especially good at price reduction, and has little cooperation with AAK, basically small quantities of high requirement hydraulic valves. 1 year ago, she wanted us to develop a high requirement hydraulic flow control valve and promised that there will be big qty of reorders. After the trial order was sent, there was still no reorder, and I didn't want to push. In her email last month, she said that 160 hydraulic flow control valves tested last year were needed, and the price was required to be maintained and the fastest delivery time was required. This hydraulic flow control valve was used in hydraulic bending machine equipment, and the early test run was very smooth. The equipment was sold very well. Unexpectedly, 3 months later, customers complained about the weakness of the hydraulic system of the bending machine. Some valve spools and valve bodies of the hydraulic flow control valves were worn, causing leakage, resulting in the weakness of hydraulic system of bending machine. The original hydraulic flow control valve manufacturer believed that the bending machine was used with high frequency, so a small proportion of wear was normal, but Margaret's supervisor didn't think so. He predicted that there would be more and more complaints later. In fact, what his supervisor predicted was right. Margaret had to change the manufacturer. She contacted many manufacturers, but none of them was willing to develop it because of the small quantity or they couldn't meet her requirements. Margaret was worried at this time. Until receiving her email, I just knew that this hydraulic flow control valve had reorders, but were not placed with AAK, she came to me this time because she had no way. Frankly speaking, although AAK had existing procedures, I didn't want to produce this order for 160 pcs of quantity. It was not until her boss found my boss 3 days later that I gave a 1 month production time and a 50% increase in the quotation. Margaret still approved our S/C. She was criticized by her boss because they not only lost the payment to the original hydraulic flow control valve manufacturer, but also undertook an additional 50%. I estimate that Margaret will never dare to transfer the order of AAK again. I was thinking that if your hydraulic valve manufacturing quality and service level are high, in the communication with customers, you can be polite and dignified, neither humble nor overbearing, otherwise the customers don't take you seriously. The business should be done standing. Although AAK price of this hydraulic flow control valve has been increased by 50%, it has taught Margaret and me a lesson. I sent out 160 hydraulic flow control valves in only 2 weeks. Margaret was very grateful for my advance shipping, and we had mended the fences between us.
The hydraulic directional control valve with internal leakage of 2drops/min makes AAK have no peers Oliver comes from a hydraulic equipment company in Canada. At the end of last year, they planned to develop a hydraulic cylinder that uses a hydraulic directional control valve. The parameter requirements are high, especially the internal leakage should be less than 2drops/min. Oliver inquired about more than 10 manufacturers of hydraulic directional control valves. Only one supplier who had cooperated for 5 years told him that he was 90% sure. Other manufacturers surrendered. One month later, the hydraulic directional control valve was installed with the oil cylinder. Less than 12 hours after startup, the hydraulic oil cylinder was unstable during reciprocating motion. After disassembly, the engineer found that the hydraulic directional control valve had internal leakage exceeding the requirement of 2 drops/min. Oliver was very helpless. He continued to look for new manufacturers of hydraulic directional control valves, and they all basically replied that they could not meet the requirement of internal leakage. Oliver found an article on Google, "The internal leakage index is equaled to the local manufacturer in Germany, but AAK hydraulic threaded cartridge valve has better cost performanceâ??, and left a message on our website: can you customize the hydraulic directional control valve with internal leakage of 2drops/min? At first glance, I knew that this was an accurate customer consultation. Although the internal leakage of 2drops/min was difficult, AAK had mass production 1 year ago. We suggested him send us the drawings and working condition requirements of the hydraulic directional control valve, and AAK can make samples directly. If the internal leakage of the hydraulic directional control valve does not meet the standard, 100% of the development cost will be returned. According to the development data provided by Oliver, there may not be any other manufacturer that can provide guarantee except AAK. After 30 days, AAK successfully sent 8 hydraulic directional control valve samples. Three months later, Oliver informed that no abnormality of the hydraulic directional control valve was found during the 3 internal commissioning of his company. After the hydraulic cylinder was tried out by the user, the feedback was also very good. Oliver is curious about the hydraulic directional control valves surrendered by so many manufacturers. Why did AAK samples succeed at one time? AAK hydraulic directional control valve has 3 absolute advantages and has already surpassed its domestic counterparts: 1. The precision honing machine imported from the United States is used to finish the valve hole and valve spool of the hydraulic direction control valves for more than 3 times. The dimensional accuracy of the valve hole is IT7 ~ 4, and the surface roughness can reach Ra 0.32 ~ 0.04�¼m, thus meeting the requirements of high accuracy.
Customer reversed internal and external leakage of the hydraulic directional control valve, causing vibration, AAK new design solved it all at once Stephen is from Hi-Force hydraulic equipment manufacturing company in the UK. In the second half of last year, he was promoted to the purchasing manager of Kuala Lumpur Branch due to his excellent work. Within a week of taking office, he met with complaints. A batch of their hydraulic cylinders were noisy and vibrated seriously during operation. The after-sales engineer failed to solve the problem within 3 days. The user was not satisfied. Stephen was a little worried. Stephen browsed an article of AAK on Google: "change the design of the hydraulic directional control valve, the vibration disappeared, and AAK eliminated the Canadian factory at zero cost", and left a message: how to solve the noise and vibration of the hydraulic cylinder? After reading this message, I roughly judged that either the hydraulic directional control valve used had problems or the original design had hidden dangers. We asked Stephen to provide the hydraulic system schematic diagram and design drawings, and AAK engineer judges that the working principle of the hydraulic cylinder is reasonable, only by checking on site can we find out the source of the vibration, and then no news from Stephen. 2 weeks later, Stephen emailed that according to the last case that AAK solved the vibration of the hydraulic cylinder, they also added a triangular throttling groove to the hydraulic direction control valve, but after installation, the hydraulic cylinder still vibrated. Their engineers said that AAK solution was a lie. I was speechless and didn't want to explain anything, so I ignored him. 3 days later, Stephen emailed us again, and sent a video of the hydraulic cylinder working and asked our help to check. AAK engineers found that the hydraulic cylinder will emit rhythmic noise and vibration whenever the load drops in the actual work, and preliminarily judged that there is a problem with the hydraulic direction control valve. AAK technical team discussed again according to the drawings, the working principle diagram of the hydraulic cylinder and the working video of the hydraulic cylinder, and confirmed that the problem lies in the hydraulic direction control valve. I told him that AAK could redesign the hydraulic directional control valve and asked him to send us samples of the original hydraulic directional control valve. Stephen may have no choice but promised. 5 days later, we received the sample of the original hydraulic directional control valve, which confirmed the judgment of our engineers that the internal leakage and external leakage of the original hydraulic directional control valve was reversed. 1 week later, AAK sent the newly designed external leakage type hydraulic directional control valve. Stephen informed by email that the noise and vibration problems of the hydraulic cylinder had been
AAK hydraulic directional control valve, which has been used for 2 years, is free of rust and corrosion. It stands out from 3 hydraulic valve manufacturers. Joseph finally received a large order for 1000 hydraulic directional control valves from customer. Joseph is the purchasing manager of a hydraulic pump company in Italy. Two years ago, the company received a test order for a special chemical hydraulic pump, which needs a hydraulic direction control valve. The customer requires that after 2 years, if the hydraulic directional control valve is free of rust and corrosion, it will have the opportunity to obtain a large order. The boss asked Joseph to find a very professional hydraulic valve manufacturer. Joseph knew that relying only on the existing hydraulic valve suppliers is not enough to guarantee the quality. He checked with all the hydraulic valve manufacturers he had contacted before and the new ones searched online, and selected 16 hydraulic valve factories, including AAK Hydraulic Valve. He asked all hydraulic valve manufacturers to provide 2 samples of hydraulic directional control valves according to the drawing requirements of the customer for testing at their headquarters. According to the post analysis to the drawing of hydraulic directional control valve from Joseph, we found that there is no problem to meet the accuracy, sensitivity and durability of this hydraulic directional control valve, except that the finish of the outer surface of the hydraulic directional control valve must be free of abnormality, rust and corrosion after 2 years of use, which is too uncertain. We didn't receive email from Joseph until 15 days after we sent out the hydraulic directional control valve samples. According to their simulation test, only the hydraulic directional control valves from 3 factories can be approved to send samples to their customer. It would take 2 years for AAK to know if we can get the order of hydraulic directional control valve. At that time, we were very surprised that there were such strange customers. We almost forgot the test order of this hydraulic directional control valve 2 years ago. Last week, Joseph sent an email asking about the production time and new price of 1000 hydraulic directional control valves, and told us that the surface of the hydraulic directional control valves from other two hydraulic valve manufacturers began to have scratches, corrosion, fading and rust after more than a year of use, only the surface gloss of AAK hydraulic direction control valve does not change. In fact, when we sent out the hydraulic directional control valve samples, we were not 100% sure to meet this special requirement, because we used a new process to proofing. We know that the conventional nickel plating, chromium plating, zinc plating, blackening and other processes basically can not keep the same appearance after 2 years of use. We adopted electroless nickel plating.
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